General maintenance

Arkansas Metal Art

Well-Known Member
I recently acquired a 6x12 TMX table with a Hypertherm Powemax 125. Im in the process of returning it to its former glory. I havent seen many posts on general maintenance so I thought I'd throw up some pics of my progress. Much thanks to LECS-Chad for his help and advice.

DAE7AD1E-E44C-4B2D-B722-5FC01AF7B4BB_zpssc2pzdev.jpg


To start, the previous owner had installed a new breakaway signal cable. When re-pinning the molex connector they didn't get the pins pushed all the way in and the crimps were in bad shape. I repinned and recrimped.

I noticed the x axis motor was slipping. I removed and opened it up to find the set screw had loosened up and the shaft was spinning in the inner split collar. After a good cleaning and tightened set screws it was ready to go.
6C05833B-1810-4575-82A1-189CEA2D27E5_zps1fbyt9pt.jpg

68F93FD4-7645-4FD4-8A3B-EA0CE5ABD507_zpsqqal3uzi.jpg


Next issue was one of the y axis spur gears only engaged half of the gear rack. This was due to the previous owner installing the gear to far down on the shaft and then installing one of the brackets upside down to compensate. Unfortunately the gear was seized to the shaft so I made a plate to pull it off.
7340B301-F9AA-47D4-BA6A-C3017D1D6B00_zpsbjfump3d.jpg

FC8133A1-AE6C-48D5-85B6-C6608908E5CF_zpsphxqnlrt.jpg

B324B4E9-A470-4C0A-9002-7ECECDD9630C_zpsvrsfulwf.jpg

A little wire wheel on the bench grinder action and the shaft and gear were good as new. I went ahead and pulled the other y axis motor and gave it a good cleaning also. While I had the y axis motors out I pulled all the followers and gave them a good cleaning. Here's some before and after pics.
3C6F3083-D623-4FEA-A8FF-F79A078692C8_zpso6gsbp4x.jpg

0656BE1C-5D8B-4D78-8371-F2D4283FF43E_zpsez8nzpxq.jpg

4D57A340-569B-46F6-BDA1-848AC41AC963_zpsq3xuugqq.jpg
C3ECFE3F-7FE9-4045-96CC-49AE9696D703_zpsaoa3ljju.jpg
12736A20-5CBE-4EFE-9EFF-A92AC66A1B4E_zpstx2knm81.jpg
EB42A174-DF7D-43AA-BA76-1A109DD7EC05_zpscu4mmocw.jpg
FF686EFB-E3C4-44AA-B235-CCB00BDD380E_zpsvqgq43iz.jpg
05C011F7-9CD3-40D3-BF3C-A02EC9ADF6E2_zpsqpkcovxj.jpg
BBE97256-294A-4D0F-B603-5335B344DACF_zpsuhnyyftd.jpg
5EEFF30C-CAB1-4262-868F-9F4772B1ADC9_zps4vvhqcyi.jpg
120BD2C0-EF25-4BBB-AA20-9C2055842DE8_zpsj7hhpux1.jpg
AC6873E8-637F-4E15-8FD1-AFFE6909AC3F_zpscigpwvbk.jpg


I used 1/8" plates as temporary spacers to adjust the location of the horizontal rollers, making sure the gantry was level left to right and front to back ( I originally laser leveled the table). After getting the height I then adjusted the vertical rollers per manual instructions. If you've ever put together a small block Chevy (I say Chevy because that's the only motor worth putting together) I would compare checking the gantry side to side tolerance to checking the end play on the crank. Just enough but not to much.

I reinstalled both y axis motors and tested. Noticeable difference. It's amazing how much smoother and quieter the gantry is with the proper gear lash and all the followers cleaned.
 
Last edited:
This is great! Nice work! It's nice to see it getting all cleaned up.

Looking forward to seeing what you'll be making on this. Are you going to be making some larger sized art pieces?
 
This is great! Nice work! It's nice to see it getting all cleaned up.

Looking forward to seeing what you'll be making on this. Are you going to be making some larger sized art pieces?

Thanks. An ounce of preventative maintenance is worth a pound of tech calls. That should be LECS/Torchmates new motto. :D

In regards to your question, I have been paying a local guy to cut my larger projects. No more!! I can now be more aggressive in solicitating bigger jobs. So we'll see. Thanks.
 
"If you've ever put together a small block Chevy (I say Chevy because that's the only motor worth putting together)"

Whoa! You tryin' to start something here ? LOL

Nice resto job on the table!
 
Just got the 4400 table and going to try and keep it looking good by cleaning it once a week. I had a plasma cam table years ago and had the water level set too low so had plasma dust everywhere.
I now know i can set the water to the top and no dust. any advise on if the water splashing up while cutting is bad or ok and what is best way to clean and maintain?
Thanks
 
I use just a rag and simple green to keep our demo machines clean. Usually I give a wipe down after each day or heavy use.
 
Back
Top